Thread: my 1/2 ton GMC
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10-29-2003 05:54 AM #1
my 1/2 ton GMC
Is now back up and running after the big engine compartment burn.
Droped a 204/214 420/442 lift cam in the 305.
the holley I bought on e-bay was crap. So I rubuilt the 795cfm Quadrajet installed new metering rods from donor carbs. now it runs like raped ape.
oh to give some info it has a Wienand stealth manifold with the holey to quadrajet adapter.
The only thing now is getting the 350turbo to shift a little sooner ie 1st to 2nd is at 42mph and 2nd to 3rd is at 57mph once in 3rd I can cruise at 60mph at 2000rpm any sugestions? Oh if I engage the lock up it drops to 1800 rpm.
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10-29-2003 10:35 AM #2
vacum leak found trany shifting like butter at correct shift points.
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10-29-2003 03:22 PM #3
Are the 305 heads modified, ie larger valves? Just wunderin cause you got 795cfm, did you use an extreme energy comp cam?Justin RFFR
Isaiah 40:31
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10-29-2003 04:24 PM #4
no they are stock heads. Cam is by summit. I ran out of cash and had the carb here so that is what I used I may still put big metering rods in it to lean it out a bit more. the nice thing is that quadrajets when set up right only flow the air that the engine needs.
Great to see your new post, Mike, and great to see CHR up and running again after several days of the Hmmm, can't reach this page.... Also good that you found an easy solution to your storage/access...
1968 Plymouth Valiant 1st Gen HEMI