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Thread: 428 smokes ... #1 Cylinder only
          
   
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Argess 428 smokes ... #1 Cylinder... 07-31-2008, 02:59 PM
Geezer2 Who did the assembly work? FE... 07-31-2008, 03:21 PM
IC2 I'll agree with the water as... 07-31-2008, 04:04 PM
Argess I've tried to add to this... 08-02-2008, 01:11 PM
Argess Thanks for the reply guys. ... 08-01-2008, 04:36 AM
Argess Hmmm....I wrote a response,... 08-01-2008, 05:29 AM
Argess Hmmm....I wrote a response,... 08-01-2008, 10:12 AM
Dave Severson Sounds like you have it... 08-02-2008, 01:16 PM
Argess I thought I had it handled... 08-07-2008, 07:03 AM
IC2 I still feel that with the... 08-07-2008, 07:46 AM
Argess Thanks for the reply IC2. I... 08-07-2008, 08:43 AM
IC2 I feel for you with an FE... 08-07-2008, 09:04 AM
41willys I had that same problem with... 08-07-2008, 09:54 AM
fitzwilly Had a similar problem with a... 08-07-2008, 10:09 AM
Argess Thanks guys. No porting... 08-07-2008, 10:20 AM
Argess I thought I'd post a... 09-18-2008, 07:24 AM
IC2 Been a long process hasn't it... 09-18-2008, 08:52 AM
Argess Yes, IC2,.....it took a long... 09-18-2008, 09:14 AM
  1. #1
    fitzwilly's Avatar
    fitzwilly is offline CHR Member Visit my Photo Gallery
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    Jun 2007
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    FLUSHING, MICHIGAN
    Car Year, Make, Model: 59 FORD FAIRLANE 500 GALAXIE
    Posts
    207

    Had a similar problem with a Ford Y-block last year. After much frustration I finally found that someone in the past had ported the head and got a bit carried away and ground the intake runner paper thin. Finally it cracked and was allowing oil to be sucked into the head, causing that cylinder to smoke and fouling the plug. It wasn't in a spot that could be welded, and the owner didn't want to pay for a new head, so some careful work with some epoxy sealed the crack. A year later it's still running strong.

  2. #2
    Argess is offline CHR Member Visit my Photo Gallery
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    Jul 2008
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    P'ville
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    Thanks guys. No porting done, so hopefully stock heads are thick enough, although a crack did occur to me. I did look at the underside of the manifold for cracks and didn't see any, but that certainly doesn't mean there isn't one. It did look a bit "wet" looking up the manifold intake runner.

    I wonder how they check aluminum for cracks.....I doubt magnafluxing would work..... And it's not a Ford manifold....it's a 2x4 360Deg Offenhauser, so "readily available" is not likely. Bad port matching anyway......would try to find a different 2x4 manifold....mind you, then there's that epoxy idea.....

    anyways, you guys are right....I need to do a close inspection for manifold cracks.......thank-you

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