Thread: Roger's LARS Mis-Adventure 2014
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06-10-2014 10:02 AM #19
Well.. I want to say that's good news.. but, not really HUH?At least "we" can explain most of it..
Have you put a torque wrench on the crank and done a torque reading? I am assuming Scott did originally... Your new value should be lower due to wear / break-in... it "may" give an indication of bearing condition..
Again, grasping for straws..
What head gaskets had been in use? Were they Fel-Pro?
Looks Factory!!
1968 Plymouth Valiant 1st Gen HEMI